January 16, 2000 NTSB Incident Report on the Beech 23 at Loris, SC (ATL84FA090) |
|
January 16, 2000
| by |
The Editors of AVweb |
| Documents Provided by the NTSB
|
NTSB Identification: ATL84FA090
For details, refer to NTSB microfiche number 24501A
Accident occurred FEB-01-84 at LORIS, SC
Aircraft: BEECH 23, registration: N6141N
Injuries: 4 Fatal.
THE ESTIMATED TIME OF TAKEOFF WAS ABOUT 1930 EST. THE ROUTE OF FLT BEFORE 2000 EST WAS
NOT KNOWN. AT APRX 2005, THE PLT REPORTED THAT HE WAS UNSURE OF HIS POSITION. SHORTLY
AFTER THAT, THE ACFT WAS IDENTIFIED OVER A MILITARY FIRING RANGE. THE PLT WAS VECTORED
FROM THE RANGE TOWARD OCEAN ISLE, NC. AT 2052, THE PLT ACKNOWLEDGED INSTRUCTIONS TO CHANGE
TO MYRTLE BEACH APCH CONTROL FREQ, BUT HE DID NOT CONTACT APCH CONTROL. SUBSEQUENTLY, A
FEMALE PASSENGER RADIOED THAT THE PLT WAS UNCONSCIOUS & THAT THEY WERE LOST. ATC &
THE PLT OF ANOTHER ACFT TRIED TO ASSIST, BUT THE PASSENGER WAS EXTREMELY EXCITED &
COMMUNICATION WITH HER WAS VERY DIFFICULT. THE PLT OF THE OTHER ACFT THOUGHT HE HEARD A
MALE VOICE IN THE BACKGROUND STATE "GIVE ME SOME AIR." SUBSEQUENTLY, THE ACFT
CRASHED (AT NIGHT) WHILE IN A STEEP NOSE DOWN. SLIGHTLY INVERTED, R WING LOW ATTITUDE.
TOXICOLOGICAL TESTS SHOWED THAT THE PLT & 3 PASSENGERS HAD THE FOLLOWING CARBON
MONOXIDE LEVELS: 24%, 22%, 35% & 44%. THE EXACT POSITION OF A CARBON MONOXIDE LEAK WAS
NOT FOUND.
Probable Cause
Exhaust system..Leak
Incapacitation(carbon monoxide)..Pilot in command
Contributing Factors
Light condition..Dark night
Physical impairment(carbon monoxide)..Pilot in command
|