October 19, 1997 USAir 427: US Airways' View of the Accident |
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October 19, 1997
US AIRWAYS
PARTY SUBMISSION OF US AIRWAYS, INC. TO THE NATIONAL
TRANSPORTATION SAFETY BOARD
USAIR FLIGHT 427 SEPTEMBER 8, 1994 ALIQUIPPA,
PENNSYLVANIA DCA-94-MA-076 SUBMITTED SEPTEMBER 30, 1997
TABLE OF CONTENTS
- INTRODUCTION
- EXECUTIVE SUMMARY
- ACCIDENT SUMMARY
- INVESTIGATION AND ANALYSIS
- FLIGHT CREW QUALIFICATIONS
- FLIGHT CREW PERFORMANCE
- Flight Crew Control Inputs
- Flight Crew Response to Full Left Rudder Deflection
- CONCLUSIONS
- FACTUAL INFORMATION
- HISTORY OF USAIR FLIGHT 427
- INVESTIGATION AND ANALYSIS
- FLIGHT CREW QUALIFICATIONS
- CAPTAIN PETER GERMANO
- Factual Investigation
- Analysis
- FIRST OFFICER CHARLES B. EMMETT
- Factual Investigation
- Analysis
- FLIGHT CREW PERFORMANCE
- FLIGHT CREW CONTROL INPUTS
- Wake Vortex Encounter
- Disorientation and Vestibular Effects
- Speech Patterns
- Rudder Pedal Damage Patterns
- FLIGHT CREW RESPONSE TO FULL-LEFT RUDDER DEFLECTION
- Crossover Speed
- Unusual Attitude Training
- CONCLUSIONS
POST-HEARING SUBMISSION OF US AIRWAYS. INC.
USAir Flight 427
Crash Near Aliquippa, Pennsylvania
September 8, 1994
I. INTRODUCTION
The purpose of this submission is to provide the National Transportation
Safety Board with US Airways' analysis and conclusions regarding the
circumstances and causes of the crash of USAir Flight 427. As the investigation
is ongoing, US Airways reserves the right to supplement this submission.
This extensive, three-year investigation has yielded a great deal of
information and analysis. The data demonstrates, and all parties seem to agree,
that USAir Flight 427's rudder moved to a full-left position shortly after the
aircraft encountered wake vortices generated by a preceding aircraft. It is also
clear that the wake vortex encounter did not directly cause the accident.
The investigation revealed that the Boeing 737 rudder control system has
certain anomalies which may have resulted in a rudder reversal or uncommanded
full rudder deflection on the accident aircraft. As a result, the Board has
issued recommendations to correct problems that might exist in the Boeing 737
rudder control system. In addition, US Airways has implemented procedures to
deal with potential rudder control problems in the unlikely event they should
occur.
This submission does not analyze possible accident causes that were
investigated and found not to be a factor, for they are quite numerous and
undisputed. Similarly, this submission does not analyze the various possible
rudder control system failure modes because the investigation of this issue is
ongoing and modifications of that system already recommended by the Safety Board
should protect against future accidents. Instead, this submission concentrates
on the actions of the flight crew and facts which establish that the flight crew
did not cause the full-left rudder deflection, and that they acted properly in
responding to this emergency
II. EXECUTIVE SUMMARY
A. ACCIDENT SUMMARYOn September 8, 1997, USAir Flight 427 was
approaching the Pittsburgh International Airport at 6,000 feet and 190 knots
when it encountered the wake vortices of a preceding Boeing 727. Approximately
three seconds after encountering the wake vortex, the accident aircraft's rudder
suddenly moved to a full-left position. The aircraft began to yaw and roll left,
and the nose began to drop. As the crew attempted to regain control of the
aircraft, the roll and yaw continued, and the nose continued to drop.
Approximately 23 seconds after the onset of the full rudder deflection, the
aircraft impacted the ground in a nearly vertical attitude, still rolling and
yawing.
B. INVESTIGATION AND ANALYSIS1. FLIGHT CREW QUALIFICATIONSThe
flight crew of USAir Plight 427, Captain Peter Germano and First Officer Charles
Emmett, were experienced, highly qualified and fully trained pilots. They had a
combined total of over 14,000 hours of flight time as USAir pilots, including
nearly 8,000 hours in the Boeing 737. Captain Germano had flown with USAir for
over 13 years, and First Officer Emmett for seven years. Each had extensive
aviation experience prior to their USAir employment. USAir flight training
records and interviews with other pilots confirmed that the USAir 427 flight
crew were properly trained, capable, well-respected, and approached their duties
with exemplary professionalism.
2. FLIGHT CREW PERFORMANCEThe Aircraft Performance Group and Human
Performance Group studied several aspects of aircraft and pilot performance in
an attempt to determine whether the flight crew had commanded the full-left
rudder deflection that caused the aircraft to begin its yaw and roll upset and,
regardless of the cause of the rudder deflection, whether the flight crew acted
properly in dealing with the emergency. To make this determination, the Aircraft
and Human Performance Groups investigated several possible indicators of crew
actions, including wake vortex encounters, disorientation and vestibular
effects, speech patterns, rudder pedal damage patterns, B-737 crossover speeds,
and unusual attitude training and procedures.
a. Flight Crew Control Inputs
The facts developed in this investigation do not support a conclusion that
the flight crew commanded the full-left rudder deflection that caused this
accident.
The Aircraft Performance Group conducted flight tests to determine the
reaction of a Boeing 737 when flown into the wake vortices of a Boeing 727 under
the same conditions that prevailed at the time of the USAir Flight 427 accident.
These test encounters resulted in aircraft attitude deviations almost identical
to those experienced by Flight 427 during its wake vortex encounter. The pilots
who flew the tests reported that the wake vortex encounters were easily
recoverable and were not disorienting. They also reported that at no time
did they feel they were close to losing control of the Boeing 737. An airline
pilot with extensive experience in the Boeing 737 participated in the tests and
reported that the test encounters were virtually identical to those he had
experienced while flying the line, and that such encounters are frequent and
routine for airline pilots. The flight tests showed it to be extremely unlikely
that the highlyexperienced USAir Flight 427 flight crew were so startled by a
routine wake vortex encounter that they mistakenly applied and held full-left
rudder and full-right aileron for 23 seconds as the aircraft spiralled into the
ground.The Human Performance Group examined, with the aid of a NASA expert, the
possibility that Captain Germano and First Officer Emmett may have become
disoriented during the wake vortex encounter, leading to an incorrect
application of flight controls. They found that circumstances conducive to
vestibular disorientation — lack of visual references combined with sudden,
violent aircraft motion or subtle, gradual aircraft motion — were absent during
the USAir Flight 427 accident. In addition, the cockpit voice recorder tape
revealed the pilots were aware of the aircraft's attitude, but could not control
it. Because the circumstances giving rise to disorientation were not present,
and the pilots were aware of the aircraft's attitude, there is no reason to
suspect that Captain Germano or First Officer Emmett were disoriented during the
accident sequence.The high quality of the Cockpit Voice Recorder tape made it
possible to conduct a detailed analysis of the voices of Captain Germano and
First Officer Emmett during the accident sequence. The Human Performance Group's
analysis, conducted with the assistance of three experts in the field, showed
that First Officer Emmett was flying the aircraft. The analysis also showed that
Captain Gerrnano was not participating in physical control of the aircraft until
immediately prior to impact, if at all. The voice analysis shows that Captain
Germano was attempting to analyze the nature of the problem while directing the
recovery attempt. There is no evidence that both pilots attempted to
simultaneously apply flight control inputs during the wake vortex encounter or
the full rudder deflection that followed.
The cockpit voice recorder also shows that the pilots' voices during the wake
vortex encounter were unexcited. Even several seconds after the onset of the
full rudder deflection, their voices still did not demonstrate "startle" or
panic. The voice analysis studies provide no evidence that the flight crew were
so startled by their wake vortex encounter that they unknowingly and incorrectly
applied full rudder, full opposite aileron, and held these cross-controlled
inputs for 23 seconds as the aircraft spiralled into the ground.b. Flight
Crew Response to Full-Left Rudder DeflectionAnalysis and flight tests
conducted after the accident revealed that at the time of the wake vortex
encounter, USAir Flight 427, although flying at the correct airspeed, was
nonetheless flying at an airspeed below which the Boeing 737's lateral controls
(ailerons and spoilers) were unable to overcome the roll induced by a
fully-deflected rudder. This latter speed is known as the "crossover speed,"
although the term and the concept had not been made known to USAir or the
airline industry prior to this accident. Below the crossover speed, an aircraft
that experiences an uncommanded, fully-deflected rudder cannot be recovered
unless the crew accelerates the aircraft to a speed above the crossover speed,
which requires that the crew immediately descend toward the ground to gain speed
as quickly as possible. Such a maneuver under the circumstances would be
completely inconsistent with training, pilot instincts and expectations, unless
the crew had been aware of the crossover speed concept and the crossover speed
for their flight configuration.
Post-accident analysis showed That Flight 427's rudder moved to a
fully-deflected position while the aircraft was at or below the crossover speed.
Upon encountering this uncommanded yaw and roll, the flight crew reacted
properly by applying aileron and spoiler opposite the direction of the
uncommanded yaw and roll. The crew, unaware of the crossover speed concept, let
alone the B-737's crossover speed, attempted to maintain altitude while
recovering from the uncommanded yaw and roll. These actions were proper and
consistent with existing knowledge and procedures but, unbeknownst to the flight
crow, quickly placed the aircraft in a position from which recovery was not
possible.C. CONClUSIONSThe data revealed during this investigation demonstrates
that Captain Germano and First Officer Emmett did not apply full-left rudder
during the wake vortex encounter, oppose it with opposite aileron and spoiler,
and hold these cross-controlled positions for 23 seconds as the aircraft
spiralled into the ground. The investigation did, however, reveal several
anomalies the Boeing 737 rudder control system that may have caused the
aircraft's rudder to fully deflect without crew input or to move opposite to the
crew's input.For these reasons, US Airways concludes that the probable cusee of
the accident was an uncommanded, full rudder deflection or rudder reversal that
placed the aircraft in a flight regime from which recovery was not possible
using techniques known at the time. Contributing to the accident was the failure
of the manufacturer to advise operators of the 737 that there were speeds below
which the ailerons and spoilers could not counteract a hardover rudder.
III. FACTUAL INFORMATION
A. HISTORY OF USAIR FLIGHT 427
On September 8, 1994 at approximately 1903 Eastern Daylight Time, USAir
Flight 427, a regularly scheduled revenue flight from Chicago, Illinois to
Pittsburgh, Pennsylvania, crashed while approaching the Greater Pittsburgh
International Airport.The Captain, Peter Germano, and the First Officer, Charles
B. Emmett, III, were on the last day of a three-day trip at the time of the
accident. The accident flight was their tenth flight together during the trip.
Between them, these pilots had over 40 years of aviation experience and over
21,000 flight hours, approximately 7,700 of which were in the Boeing 737.During
the trip, the crew's on-duty time had never exceeded nine hours during any one
day, and off-duty time had never been less than 13 hours between duty periods.
Human Performance Group Factual Report, Exhibit 14A at 4.Captain William
Jackson, a USAir DC-9 Captain, flew in the cockpit observer seat ("jumpseat")
during the flight from Charlotte, North Carolina to Chicago, Illinois, which
immediately preceded the accident flight. Testimony of Captain William Jackson,
Transcript of Proceedings before the National Transportation Safety Board,
January 23, 1995, 41 (hereinafter, "Jackson Tr."). Captain Jackson stated that
Captain Germano flew the leg from Charlotte to Chicago. Operations Group Report,
Exhibit 2A at 3. He described the crew as "capable and very professional" and
reported they used aircraft checklists and made all the standard and required
call-outs. Jackson Tr. at 47. Captain Jackson is experienced on the B737-300,
having Hown 2,800 hours in that aircraft as both Captain and First Officer.
Id. at 49.
He did not observe any aircraft problems and did not see any outstanding
Minimum Equipment List notations in the cockpit. Id. at 45-46.The
aircraft, a Boeing 737-300, Registration Number N513AU, was on its seventh
flight of the day when the accident occurred. There had been no discrepancies
reported on any of the previous flights, and there were no outstanding Minimum
Equipment List items. Operations Group Report, Exhibit 2A at 3. The aircraft's
inspections were current, including three rudder functional inspections required
by Airworthiness Directive AD 94-01-07 during the previous six months.
Maintenance Records Group Chairman's Factual Report, October 14, 1994, Exhibit 1
1A at 4.The departure from Chicago and flight into the Pittsburgh area were
uneventful. Air traffic control tapes and the Cockpit Voice Recorder indicate
First Officer Emmett was flying this leg. Operations Group Report at 4. External
and intra-cockpit communications were routine, including appropriate reading of
checklists. Id. The weather was clear, it was still daylight, and there
was a distinct horizon.At 1902 EDT, Pittsburgh Approach Control directed USAir
Flight 427 to turn left to a heading of 100°. As previously directed by Air
Traffic Control, USAir Flight 427 was level at 6,000 feet (MSL) and maintaining
190 knots indicated airspeed. The landing gear was up with Flaps 1 selected and
the autopilot engaged. The accident aircraft was 4.2 miles behind a Boeing 727
aircraft, Delta Airlines Flight 1083, which was descending to 6,000 feet. The
two aircraft were assigned the same heading.
As USAir Flight 427 approached its assigned heading of 100° and had almost
rolled out of its slight left bank, the flight data recorder showed small
changes in airspeed, attitude, and vertical acceleration.1 The
autopilot was still engaged. Within a second, the cockpit voice recorder
recorded comments by the pilots ("Sheez"; "Zuh") and a thump on the aircraft.
Over the next three seconds, the aircraft rolled left to approximately 18° of
bank, then rolled slightly back to the right, but never reached a wings level
attitude. During this three seconds, the CVR recorded another thump on the
aircraft. The Captain commented, "Whoa," and the CVR recorded the sound of the
aircraft trim wheel turning at autopilot trim rates. The FDR recorded an
increase in the amount of aft control column being commanded as the autopilot
maintained level flight.At 1903:01 EDT, the aircraft's heading slewed suddenly
and dramatically to the left. The Captain said, "Hang on," and the CVR recorded
the sound of the First Officer grunting.
One second after the onset of the sudden yaw, the Captain said, "Hang on"
again as the left yaw continued. The aircraft's roll attitude, which previously
had begun to decrease, suddenly began to increase to the left and reached 30°.
The aircraft's pitch attitude began to decrease rapidly. At this point, the rate
of descent was approximately 2,400 feet per minute ("fpm"). The CVR recorded the
sound of the autopilot being disconnected.One second later, two seconds after
the onset of the yaw event, the Captain again said, "Hang on." The left yaw and
roll continued, and two seconds later (1903:05), the aircraft passed 55° of left
bank, still rolling and yawing. The nose was now 10° below the horizon. The
Captain again said, "Hang on. " The rate of descent at this point was
approximately 3,000 fpm. The control column was moving aft and vertical "G"
loading increased.
1 All flight parameters noted in this submission are
from the Group Chairman's Report of Investigation, Flight Data Recorder Factual
Report, November 28, 1994, Exhibit 10A, Attachment IV. Cockpit Voice Recorder
data are taken from the Specialist's Factual Report of Investigation, Cockpit
Voice Recorder, October 5, 1994, Exhibit 12.
At 1903:07, six seconds after the onset of the yaw, the aircraft's pitch
attitude was approaching 20 degrees below the horizon. The left bank had
increased to 70°. The descent rate was now approximately 3,600 fpm. At this
point, the aircraft stalled. Left roll and yaw continued, and the aircraft
rolled through inverted flight as the nose reached 90° down, approximately 3,600
feet above the ground.The aircraft continued to roll after reaching a vertical
dive, but the nose began to rise. Approximately 2,000 feet above the terrain, as
the aircraft's attitude passed 40° nose low and 15° of left bank, the left roll
hesitated briefly. At this point, approximately five seconds prior to impact,
the Captain said, "Pull," but the aircraft immediately resumed its left roll,
and the nose again dropped. Five seconds later, the aircraft impacted the ground
in nearly 80° of dive, almost 60° of left bank, and at 261 knots indicated
airspeed. The 132 passengers and crewmembers aboard the aircraft were killed.
- INVESTIGATION AND ANALYSIS
- FLIGHT CREW QUALIFICATIONS
- CAPTAIN PETER GERMANO
a. Factual InvestigationAt the time of the USAir Flight 427 accident,
Captain Germano had accumulated 9,112 hours at USAir. He had accumulated 4,064
hours in the Boeing 737, of which 3,296 were flown as a Captain. Operations
Group Factual Report, Exhibit 2A, at 7. Captain Gerrnano's lifetime flight
experience in all aircraft was approximately 12,000 hours. Id.Captain
Germano was 45 years old at the time of the accident. Id. at 5. His
flying career began at age 20 in 1969, when he received his Private Pilot
Certificate from the FAA.
Id. at 5. He completed United States Air Force ("USAF") pilot training
in December 1973. Human Performance Group Chairman's Factual Report, Second
Addendum, October 5, 1995 at 5. Although USAF flight records from that period
are not available, the syllabus for USAF pilot training at the time required
that each student receive extensive instruction and demonstrate proficiency in
spin recoveries, unusual attitude recoveries, and acrobatic maneuvers. Human
Performance Group Chairman's Factual Report, Third Addendum, October 27, 1995 at
2.Following USAF pilot training, Captain Germano flew the 0-2 aircraft, the USAF
version of the Cessna 337. Id. The aircraft was used in the Forward Air
Controller role, which required abrupt maneuvers and rapid changes in aircraft
attitude, often at low altitude. Id. at 2-3. Captain Germano flew the 0-2
from February 1974 to March 1979, logging over 500 hours as Pilot in Command.
Human Performance Group Factual Report, Second Addendum, Exhibit 14X-A, at
5.Captain Germano received his Commercial Pilot Certificate in 1974. Operations
Group Factual Report at 5. Prior to his employment at USAir, Captain Germano was
a flight engineer for Braniff Airlines. Human Performance Group Factual Report,
Second Addendum, at 5. Captain Gerrnano was hired by USAir in 1981 as a B-727
Second Officer, then progressed to become a BAC 1-11 First Officer, a B-737
First Officer, and then a B-737 Captain.
The Operations Group gathered evaluator comments on Captain Germano's most
recent training and evaluation events, as well as post-accident peer reports.
Captain Germano had received five simulator evaluations and training sessions in
the 13 months preceding the accident. Operations Group Factual Report, Exhibit
2A, at 6. In each of these training sessions and evaluations, he successfully
completed all the required tasks without a discrepancy. There were no negative
comments on Captain Germano's performance from any of the five Check Airmen who
administered these evaluations and training sessions. Id. The Check
Airman who conducted Captain Germano's requalification simulator in April 1994
reported that the training went well with no problems. Id. Similarly, the
Check Airman who flew three requalification flights with Captain Germano in May
1994 reported that Captain Germano was "very meticulous, very professional, paid
attention to detail, ran complete checklists, and followed all procedures."
Id. Three first officers who had flown with Captain Germano during the 60
days preceding the accident described him as flying "by the book" and as "very
proficient," "very thorough," and "not excitable." Two of these first officers
stated that Captain Germano's greatest strength was crew coordination.
Id.; Human Factors Group Report, Exhibit 14A, at 3. Captain William
Jackson flew in the cockpit jumpseat on the Charlotte-to-Chicago leg immediately
preceding the accident flight. He reported Captain Germano provided a thorough
jump seat briefing and invited input from the First Officer and from Captain
Jackson on procedures at Chicago, as Captain Germano had not landed there
recently. Human Performance Group Chairman's Factual Report, October 31, 1994,
Exhibit 14A, at 5. Captain Germano upgraded to B-737 Captain in September 1988.
He successfully completed each element of the required 12 hours of simulator
upgrade training and 21 supervised line check flights. Captain Germano
successfully accomplished all other training and evaluations received in the
time between his upgrade to Captain and the accident.
b. Analysis
Even as far back as his 1988 captain upgrade training, six years before the
accident, Captain Germano's training and evaluation records indicate he was a
very capable pilot.2 Comments by Check Airmen and First Officers who
evaluated or flew with Captain Germano near the time of the accident
consistently painted a picture of a mature, thorough Captain. Two first officers
reported Captain Germano's greatest strength was crew resource management. This
comment is borne out by the testimony of Captain Jackson, who witnessed Captain
Germano's use of Cockpit Resource Management techniques when he sought the
counsel of his fellow pilots before flying into the complex Chicago air traffic
environment.Captain Germano's flight training record and the testLmony of his
fellow pilots indicate he was a thorough, proficient, and disciplined captain.
In addition, Captain Germano's trading records do not indicate he ever
encountered difficulty with the application of the appropriate rudder at the
correct time, even in the numerous engine-out scenarios practiced and evaluated
during his Captain upgrade training or proficiency and recurrency training
simulators. Nor does the record indicate any difficulty with orientation or
controlling aircraft attitude during the numerous steep turns, approaches to
stalls, and other advanced maneuvers practiced and evaluated in the simulator.
To the contrary, Captain Germano's military training included unusual attitude
recoveries, acrobatics, and spin recoveries. Additionally, for five years he
flew a military mission requiring frequent abrupt changes in aircraft attitude.
To a pilot with such
2The Aviation Investigation Manual recommends the Operations Group
initially examine the pilots' training records for the preceding two years.
NTSB Aviation Investigation Manual, Vol. II, p. II-F-74. Even though
nothing in the pilots' records for the two years preceding the accident would
indicate a need to examine older records, US Airways' Submission will discuss
these pilots' records as far back as their checkouts in the positions they held
at the time of the accident.
experience, the routine wake vortex encounter experienced by USAir Flight 427
would not pose any significant difficulty in recognition or recovery.
The facts brought to light in this investigation show clearly that Captain
Germano was fully qualified and properly trained to function as the Captain of
USAir Flight 427. His training and experience indicate he possessed the skill
and training needed to recognize, analyze, and successfully recover a normally
functioning aircraft from the routine wake vortex encounter experienced by USAir
Flight 427.
2. FIRST OFFICER CHARLES B. EMMETTa. Factual Investigation
First Officer Emmett was 38 years old at the time of the accident. Human
Performance Group Factual Report, Exhibit 14A, at 3. He started taking flying
lessons as a teenager, and began his aviation career as a corporate pilot.
Id. He was hired by Piedmont Airlines (later merged with USAir) on
February 2, 1987 as a First Officer on the F-28 aircraft. At the time of the
USAir Flight 427 accident, First Officer Emmett had accumulated 4,919 hours as a
pilot with Piedmont and USAir, all of it as a First Officer. This time included
3,644 hours in the Boeing 737. Operations Group Chairman's Report, Exhibit 2A at
9. In all, he had accumulated over 9,000 hours in his flying career Id.
First Officer Emmett received three evaluations and training sessions in the
seventeen months preceding the USAir Flight 427 crash. FIe completed each of
these evaluations without a discrepancy. Id. The Check Airman who
administered First Officer Emanett's last Proficiency
Training session in the simulator on May 12, 1994 recalled that First Officer
Emmett was well prepared for the training and that his performance in the flying
and oral evaluations was "sharp. " Id.
A month before the USAir Flight 427 accident, First Officer Emmett was the
"pilot flying" when the B-737 he was flying experienced a hydraulic system
failure necessitating a heavyweight precautionary landing. Human Performance
Group Chairman's Factual Report, October 31, 1994, Exhibit 14A, at 3. During the
incident, First Officer Emmett transferred aircraft control to the captain, then
assisted the captain in executing diagnostics and accomplishing the successful
heavyweight landing. Id. The captain described First Officer Emmett's
performance during the incident as "great," and indicated First Officer Emmett
was calm throughout the situation. Id.; Operations Group Chairman's
Factual Report, Exhibit 2A at 9. Other Captains who had flown with First Officer
Emmett within the 60 days preceding the accident described his piloting skills
as "exceptional" and his performance as "outstanding." Operations Group Report,
Exhibit 2A, at 9.
First Officer Emmett's transition training into the Boeing 737 began in April
1989. He received four simulator practice sessions, all elements of which he
performed without a discrepancy. As part of the transition training, he received
12 Initial Operating Experience evaluation flights in the B-737, all of which he
also completed without a discrepancy. On May 1, 1989, First Officer Emmett
successfully completed his B-737 Transition Proficiency Check, again without a
discrepancy. On May 8, 1989, First Officer Emmett completed four hours of Line
Oriented Flight Training (LOFT), which was graded Satisfactory without comment.
b. Analysis
Check Airmen and Captains who flew with First Officer Emmett within the 60
days prior to the accident praised First Officer Enunett's flying skills as
"exceptional." His flight training record supports that conclusion. His flying
record does not indicate any difficulty with making appropriate flight control
inputs at the correct time. Nor does the record indicate any difficulty with
orientation or controlling aircraft attitude. Throughout his seven-year career
with USAir, First Officer Emmett, like Captain Germano, had successfully
completed numerous training sessions and evaluations that included single engine
maneuvering, steep turns, and other high task load events with significant
potential for disorientation or confusion.
First Officer Emmett was fully trained and qualified to function as the First
Officer aboard USAir Flight 427. His calm performance during the hydraulic
failure incident only a month before the accident further demonstrates his
flying proficiency and knowledge of proper crew coordination techniques. From
his reported "exceptional" flying skills to his recent performance as a first
officer, everything in First Officer Emmett's flying record indicates he was
fully able to recognize, analyze, and successfully recover a normally
functioning aircraft from the routine wake vortex encounter experienced by USAir
Flight 427.B. FLIGHT CREW PERFORMANCEThe investigation focused on two aspects of
the performance of Captain Gerrnano and First Officer Emmett during their
encounter with wake vortex and the subsequent uncommanded full rudder deflection
that caused this accident. The investigation examined whether the flight crew
was the source of the full rudder movement and, whatever the source of the
movement, whether the crew used proper recovery technique during the ensuing
upset.
1. FLIGHT CREW CONTROL INPUTS
The Aircraft Performance Group concentrated its investigation on
reconstructing the flight control inputs made during the accident sequence. Part
of that effort included study of the effect of a Boeing 727's wake vortex on a
Boeing 737. The Human Performance Group's efforts included study of the pilots'
backgrounds and the actions of the pilots in the final moments of flight. Human
Performance Group Chairman's Factual Report, Second Addendum, October 5, 1995,
Exhibit 14X-A, at 2.
One question examined by these Groups was whether the flight crew commanded
full-left rudder in reaction to the wake vortex then continued to command
full-left rudder for 23 seconds while simultaneously attempting to overcome the
rudder deflection with opposite aileron as the aircraft spiralled into the
ground. The Aircraft Performance and Human Performance Groups investigated
several areas in an attempt to determine if the full rudder deflection that
caused this crash was commanded by the flight crew. Moreover, the Boeing Company
provided the Human Performance Group and the Board with memoranda and a
"contribution" intended to support the theory that Captain Germano and First
Officer Emmett were so "startled" by a routine wake vortex encounter that they
input full rudder and held it until the aircraft impacted the ground. As the
following analysis shows, there is no evidence to support the theory that a
pilotcommanded rudder deflection caused this accident.
a. Wake Vortex Encounteri. Introduction
USAir Flight 427's wake vortex encounter has relevance to the accident
investigation only to the extent that it caused a momentary rudder input (by the
flight crew or through the yaw damper) which, due to an unknown mechanical
malfunction, translated into a hardover or reversed rudder. The facts of the
investigation do not support an inference that the continuous, full rudder
deflection which occurred subsequent to USAir Flight 427's encounter with wake
vortex was commanded by the flight crew.
ii. Factual Investigation
Radar data obtained during the investigation showed that at the time of the
onset of the accident event, USAir Flight 427 was approximately 4.2 miles behind
a Boeing 727 aircraft, Delta Flight 1083, which was flying approximately the
same heading. The descent profiles of the two aircraft momentarily placed USAir
Flight 427 slightly below the flight path flown by Delta 1083. As the accident
event began, USAir Flight 427's FDR recorded slight changes in airspeed,
attitude, and vertical "G" forces, indicating an encounter with the wake vortex
of the preceding Boeing 727.
During its investigation of the USAir Flight 427 accident, the NTSB conducted
flight tests in which a Boeing 737-300 was flown into the wake of a preceding
Boeing 727 which had been configured with smoke generators to make the
aircraft's wake vortices visible. Group Chairman's Report of Investigation —
Wake Vortex Flight Test, November 9, 1995, Exhibit 13X-A at 2. Among the
purposes of the flights was to determine the aerodynamic effect of Boeing 727
wake vortices on a Boeing 737. Id.
Three of the pilots who participated in the wake vortex tests testified
before the Board during its public hearings. Lester Berven is the Supervisory
Flight Test Pilot in the Flight Test Branch of the FAA Aircraft Certification
Office in Seattle, Washington. Testimony of Lester Berven, November 16, 1995 at
1966 (hereinafter, "Berven Tr."). He holds a Bachelor of Science degree in
Aeronautical Engineering and has accumulated 7,000 total flying hours, of which
approximately 3,500 are in certification or engineering flight test. Id.
at 1967. He is rated in all Boeing aircraft except the B-707. Id. In
his capacity as an FAA supervisory test pilot, he flies certification flights
and supervises the activities of five other pilots. Id. He participated
in the certification of the B-737-300 aircraft in 1984. Id. at 1968.
Michael Carriker is the Senior Engineering Project Pilot for the B-737 at the
Boeing Company. Testimony of Michael Carriker, November 16, 1995 at 2083
(hereinafter, "Carriker Tr."). In that capacity, he contributes to new aircraft
projects and continuing improvements. Id. at 2084. He holds a Bachelor of
Science degree in Science and Aeronautical Engineering, was a Navy test pilot,
and is rated in all current Boeing production aircraft. Id. He has
amassed approximately 5,000 hours flight time.
Captain John Cox is a B-737 captain with USAir, and the Chairman of the
Airline Pilots' Association Central Safety Conunittee at USAir. Testimony of
Captain John M. Cox, November 16, 1995 at 2181 (hereinafter, "Cox Tr."). He has
flown professionally for approximately 22 years. Id. at 2152. He has
accumulated a total of 12,000 flight hours, of which approximately 8,000 have
been in the B-737.
Each of these pilots described the flight test wake vortex encounters. Mr.
Carriker testified that when encountering the B-727's wake vortex, the B-737
would react to the vortex
in the roll axis. Carriker Tr. at 2106. The encounters did not result in a
large or sustained yaw or a large heading change. Id. at 2109; Berven Tr.
at 2007. Each encounter resulted in a vertical G spike, followed by a rolling
moment. Carriker Tr. at 2107. At no tune did Mr. Carriker feel he was losing
control of the aircraft during these wake vortex encounters. Id. at
2110.Mr. Berven participated in the wake vortex test encounters conducted at
four and three miles behind the B-727. Berven Tr. at 2003. He noted that the
encounters with the vortex typically resulted in a 10~ to 20° excursion in bank
angle when the aircraft was being handflown or flown on the autopilot during the
encounter. Id. at 1999. The maximum bank angle Mr. Berven experienced was
30°, and that was during a wake vortex encounter flown without any pilot or
autopilot input to counter the vortex effects. Id. Mr. Berven found the
autopilot did an effective job of controlling the aircraft during the wake
vortex encounters. Id. at 2010. In encounters with the autopilot on, the
aircraft typically did not roll more than ten degrees. Id. During none of
the wake vortex encounters did Mr. Berven feel that the aircraft was out of
control or even on the verge of being out of control. Id. at 2013.
Both Mr. Berven and Captain Cox stated that staying in the vortex was
difficult because the dynamics of the aircraft and vortex resulted in the
aircraft being Spit out" of the vortex rather rapidly. Berven Tr. at 2000; Cox
Tr. at 2165. All three pilots noted that the average duration of an encounter
with a wake vortex during the test was on the order of two seconds. Berven Tr.
at 2000; Cox Tr. at 2165; Carriker Tr. at 2110. Mr. Carriker testified that it
was possible to stay in the effect for up to three or four seconds, but only if
the intent was to do so.
Carriker Tr. at 2110. Because the two wake vortices rotated in opposite
directions, transitioning from one vortex to another during an encounter tended
to correct the initial roll upset. Id.
Mr. Berven and Captain Cox also noted that wake vortex encounters are common
in line flying. Berven Tr. at 2005; Cox Tr. at 2164. Captain Cox stated that
wake vortex encounters occur on the order of two or three times during a three
or four day trip. Cox Tr at 2185. Captain Cox noted that the encounters he
witnessed during the tests were representative of the wake vortex encounters he
has experienced while flying the line. Cox Tr. at 2184. In both the tests and
line flying, the maximum bank angle he typically has seen is 20 to 25 degrees.
Cox Tr. at 2165-66. Captain Cox stated that wake vortex encounters during the
test and during line flying are "not that disruptive a condition." Id. at
2164.
During the wake vortex encounters, the yaw damper of the B-737 was providing
almost continuous input to the rudder, so much so that its input interfered with
obtaining the desired data, leading the engineers to request that the pilots
turn the yaw damper off during the encounters. Carriker Tr. at 2107. Id.
iii. Analysis
The radar, flight data recorder, and cockpit voice recorder data show that
USAir Flight 427 almost certainly encountered the wake vortex of the preceding
B-727. The radar data places USAir Flight 427 behind and slightly below
the flight path of the B-727 at the time of the onset of the accident sequence.
The FDR recorded excursions in roll, airspeed, and vertical "G" without an
accompanying pitch attitude change. The CVR recorded thumps on the aircraft
which later testing showed were consistent with the impact of a wake vortex on
the fuselage of a B-737. However, the wake vortex encounter was not the cause of
the accident.
The pilots who participated in the NTSB's wake vortex testing described the
roil rates and magnitudes they encountered, and what they described was almost
identical to the roll rates and magnitudes recorded on the USAir Flight 427
Flight Data Recorder. During the test, encounters with the wake vortex at
approximately 4 miles behind the generating aircraft resulted in roll axis
upsets of less than 25° when the autopilot was engaged, as it was on USAir
Flight 427. Like USAir Flight 427's encounter with a wake vortex, these test
encounters did not generate significant yawing moment.The USAir Flight 427 FDR
data shows that the aerodynamic reaction of the accident aircraft to its wake
vortex encounter was identical to the routine wake vortex encounters described
by Captain Cox and Mr. Berven. The maximum bank angle after the wake vortex
encounter began, and before the onset of the uncommanded yaw event, was
approximately 18°. Group Chairman's Report of Investigation, Flight Data
Recorder Factual Report, November 28, 1994, Exhibit 10A, Attachment IV. Even the
most extreme estimates of the roll rate the aircraft encountered during the wake
vortex encounter was approximately 11° per second, but the aircraft rolled less
than 10° at that rate. See, Boeing Contribution to the USAir Flight 427
Accident Investigation Board, September 25, 1996, at 4-6. Until the onset of the
full-left rudder, the maximum yaw rate during the wake vortex encounter was
negligible. Id. Until the onset of the full-left rudder, bank angle
changes during the wake vortex encounter, though rapid, were slight. The F1:)R
data clearly show the USAir Flight 427 wake vortex encounter was nothing out of
the ordinary. It was virtually identical to the types of wake vortex encounters
that are common in line flying.
Such wake vortex encounters are not unusual in line flying, and any initial
surprise experienced by the pilots on encountering a wake vortex quickly changes
to recognition, analysis, and recovery. Cox Tr. at 2170. Captain Cox, the one
pilot with extensive line flying experience who flew these tests, stated the
vortex encounters are just not that disruptive. The crew of USAir Flight 427 had
a combined total of nearly 8,000 hours of Boeing 737 time, and over 14,000 hours
as airline pilots for USAir. Captain Germano had flown the line at USAir for
over 13 years, and First Officer Emmett had flown the line for seven years. Each
had additional aviation experience prior to their USAir employment. A wake
vortex encounter would have been routine for such highly-experienced crew
members.Listening to the pilots' reactions on USAir Flight 427's Cockpit Voice
Recorder tape also reflects that these pilots were not so startled by this
routine wake vortex encounter that they applied incorrect flight control inputs
and held them. After the pilots' initial reaction ("Sheez," "Zuh"), the only
comment either pilot made before the full-left rudder began is the Captain's
comment, "Whoa. " His voice on the CVR is neither startled nor panicked; rather,
the statement is nothing more than commentary. As the event progressed from a
wake vortex encounter to an uncommanded rudder deflection or reversal, the
voices of the pilots understandably express rising concern over the performance
of the aircraft. However, an expletive spoken by First Officer Emmett some four
seconds after the onset of the unconunanded rudder deflection is made in a calm,
but concerned, tone. The evidence shows that these pilots were not so startled
by this routine wake vortex encounter that they incorrectly applied full-left
rudder, countered it with full-right aileron, then held these full
cross-controlled positions for 23 seconds while spiralling toward the ground.
Boeing's February 28, 1996 memorandum to the Chairman of the Human
Performance Group invites a chain of inferences from 44 anecdotal aircraft
incident reports concerning wake vortex encounters. The first inference invited
by this memorandum is that flight crews are commonly so "startled" by encounters
with wake vortex that they input improper flight controls or put in proper
flight controls but forget to take them out. Most of the encounters cited were
behind "heavy" category aircraft, or at short range, or at low altitude, or
under some combination of these circumstances. It should also be noted that in
the 44 reports of wake vortex encounters cited in the Boeing memorandum, only
two of the events even arguably included an incorrect application of flight
controls by a crew member. Neither of these two incident reports indicate the
crew held the incorrect input for more than a few seconds.
Relying on the same data, Boeing's September 25, 1996 "contribution" to the
Board concludes that the crew of USAir Flight 427 were "startled" by their wake
vortex encounter, leading to the incorrect application of full-left rudder and
full-right aileron until the aircraft spiralled into the ground 23 seconds
later. In support, the "contribution" breaks the movements of USAir Flight 427
during the wake vortex encounter into tenth-of-a-second increments and suggests
that the roll accelerations experienced were so far above what the crew would
normally experience that they could not cope. However, the bank angle changes
that occurred at these rates were sometimes as small as two or three degrees and
never more than 10 degrees. They were, in essence, momentary jolts rather than
dramatic, sustained accelerations.
USAir Flight 427 experienced a routine wake vortex encounter that resulted in
several rapid, small, momentary roll angle changes. The accident aircraft's roll
rates and accelerations were similar to those documented during the NTSB's wake
vortex testing. See, Group
Chairman's Report of Investigation, Wake Vortex Flight Test, Exhibit 13X-A,
November 9, 1995 at 27A - 34B. USAir Flight 427's encounter with wake vortex
resulted in the type of "bounce" or "light to moderate turbulence'' described by
the pilots who flew the wake vortex test. Carriker Tr. at 2110; Berven Tr. at
2007. Such encounters are quite common in line flying. Cox Tr. at 2185. Given
Captain Germano's and First Officer Emmett's experience, these relatively benign
motions resulting from a routine wake vortex encounter would not have led to an
extreme misapplication of flight controls.
The ultimate inference the Boeing contribution would have the Board draw is
that the crew of USAir Flight 427 applied full-left rudder during the wake
vortex encounter and held it there while applying fully cross-controlled
ailerons until impact some 23 seconds later. However, the facts revealed during
this investigation simply do not support an inference that the crew of USAir
Flight 427 reacted to the wake vortex encounter by incorrectly applying flight
control inputs. Wake vortex encounters are common events to line pilots and are
relatively benign, seldom resulting in more of an upset than 25° of bank, as was
the case with USAir Flight 427. Line pilots routinely deal with recoveries from
such encounters. Few, if any, of the reported wake vortex encounters cited to
support the inference indicate an incorrect application of flight controls,
inadvertent or otherwise. Similarly, none indicate any instance in which correct
controls were applied then inadvertently held after they were no longer needed.
Whatever the cause of the rudder deflection that led to the crash of USAir
Flight 427, there is no evidence to suggest it was an incorrect or inadvertent
pilot input brought on because the crew reacted incorrectly to a wake vortex
encounter.
B. Disorientation and Vestibular Effectsi. IntroductionThe Human
Performance Group investigated the possibility that the crew of USAir Flight 427
may have experienced spatial disorientation during the wake vortex encounter,
causing them to misapply the flight controls. The evidence discovered by the
investigation shows the pilots were not disoriented.ii. Factual
InvestigationSpatial disorientation is usually associated with degraded
out-of-cockpit vision, coupled with changes in aircraft accelerations that are
either sudden and violent or subtle and gradual. Letter from Malcolm M. Cohen,
Ph.D. to Malcolm Brenner, Ph.D., September 21, 1995, at 1 (hereinafter, "Cohen
Report"). The Human Performance Group asked Malcolm M. Cohen, Ph.D., NASA Ames
Research Center, to examine relevant information from the accident investigation
in an attempt to determine if disorientation or vestibular effects could have
played a role in the accident. Human Performance Group Chairman's Factual
Report, Second Addendum, October 5, 1995, Exhibit 14X-A, at 6. Dr. Cohen
underwent repeated simulations of the USAir Flight 427 event in the NASA
Vertical Motion Simulator, using large physical motions to produce a high
fidelity reconstruction of the event. Id.Dr. Cohen concluded that the
accident scenario did not contain evidence of the factors normally associated
with disorientation. Cohen Report at 1. The accident occurred during daylight
hours in clear air with good visibility and a clearly defined horizon. Human
Performance Group Factual Report, Exhibit 14X-A, at 6. The motion of the
aircraft after the onset of the accident event did not exhibit the types of
accelerations that would be conducive to
disorientation. Cohen Report at 2. The motions of the aircraft as the event
progressed were relatively gradual and nearly continuous. Id. The pilots'
comments indicated they were fully aware of their trajectory, but they were
unable to change it. Id. This evidence is consistent with the testimony
of two pilots who participated in the wake vortex testing, who stated that the
wake vortex encounter is not a disorienting event. Cox Tr. at 2170-71; Carriker
Tr. at 2111.iii. AnalysisDr. Cohen's analysis indicates the crew of USAir
Flight 427 were not disoriented by the wake vortex encounter that marked the
beginning of the accident sequence. The weather was clear and the horizon
distinct. The change in aircraft attitude happened gradually and continuously,
and the pilots' comments indicate they were aware of the change but could do
nothing about it. This simply was not an event that involved the sudden
placement of an aircraft in an extreme attitude, nor was it a case where subtle
changes in aircraft attitude went unnoticed by the crew until an extreme
attitude had developed. Pilots who participated in the NTSB's wake vortex
testing testified that encountering a wake vortex is not a disorienting
experience, and the facts developed during the investigation indicate the pilots
were aware of the attitude of the aircraft at all times during the accident
sequence. Therefore, disorientation was not a factor in causing this accident.
c. Speech Patternsi. IntroductionThe Human Performance Group
investigated the speech patterns of the USAir Flight 427 flight crew captured on
the Cockpit Voice Recorder. The investigation revealed, not surprisingly, that
the pilots exhibited rising stress as the accident event progressed. The
analysis also showed excellent crew coordination before and during the event and
that First Officer Emmett was physically flying the aircraft.ii. Factual
InvestigationThe Human Performance Group studied the speech patterns of the
pilots using the Cockpit Voice Recorder tape. Three consultants provided input
to the Group: an exercise physiologist who focused on breathing patterns and
physical exertion; a NASA Human Performance Researcher who focused on
intra-cockpit communication; and a Russian acoustics analyst who focused on
psychological stress and physical effort. Speech Examination Factual Report, May
5, 1997 at 5.There was no audible grunting or straining indicative of physical
exertion heard from Captain Germano before or immediately after the onset of the
accident sequence. Letter from Scott Meyer, Ph.D. to Malcolm Brenner, Ph.D.,
March 29, 1996, paragraph 7 (hereinafter, "Meyer Report"). Captain Germano's
speech patterns indicate he did not exhibit signs of physical exertion until
about 4.8 seconds prior to the aircraft's impact with the ground. This straining
may have been as a result of "G" forces on the aircraft or of his participation
in manipulating the flight controls. Letter from Alfred S. Belan to Malcolm
Brenner, Ph.D., March 26, 1997, at 3 (hereinafter, "Belan Report").
Shortly after the onset of the accident sequence First Officer Emmett made
several rapid grunting exhalations. Meyer Report at ~ 5; Belan Report at 4. In
addition, analysis of the USAir Flight 427 Cockpit Voice Recorder tape indicated
seven occasions after the accident sequence began in which First Officer Emmett
keyed the yoke-mounted radio microphone switch. Id. at 4. Human
Performance Group Chairman's Factual Report, Second Addendum, October 5, 1995,
Exhibit 14X-A, at 4. During none of these times did First Officer Emmett direct
conversation outside the aircraft. Conversely, Captain Germano keyed his
microphone switch only one time during the accident sequence, and that was to
make an emergency transmission directed to the air traffic control agency.
Id.Analysis of the intra-cockpit communications indicated there was no
reluctance of the crew to seek and incorporate information from each other, and
the level of coordination and communication was appropriate. Letter from Barbara
G. Kanlci, Ph.D. to Malcolm Brenner, Ph.D., December 2, 1996 at 3. During the
accident sequence, the Captain's comments ("Hang on"; "What the hell is this?";
"Pull") were mainly limited to commands and attempts to evaluate the situation.
Belan Report at 3.iii. AnalysisAnalysis of the CVR and air traffic
control tapes shows that First Officer Emmett was the pilot flying the aircraft
up to the time of the wake vortex encounter. After the encounter, there was no
indication on the CVR of a change of aircraft control. First Officer Emmett's
speech patterns at the beginning of the accident sequence showed forcible
exhalations indicating physical exertion. This evidence suggests First Officer
Emmett was straining while manipulating the aircraft's controls. Meyer Report at
2. Conversely, the lack of such straining in Captain
Germano's speech patterns suggests Captain Gennano was not manipulating the
controls. Further, First Officer Emmett keyed his yoke-mounted microphone switch
seven times during the accident sequence without making a deliberate
transmission. Such inadvertent microphone keying can be an indicator that a
pilot is manipulating the control wheel. Human Perfonnance Group Factual Report,
Second Addendum, Exhibit 14X-A at 3. Conversely, Captain Germano keyed his
microphone switch but once, and that was done in an attempt to notify air
traffic control of USAir Flight 427's emergency. Id. at 4. These facts
strongly infer that First Officer Emmett was manipulating the flight controls
during the wake vortex encounter and the subsequent flight control malfunction
and that Captain Germano was not.Analysis of the CVR also shows the crew used
good crew coordination throughout the accident sequence. In fact, analysis of
the entire 30-minute CVR tape showed good cockpit resource management throughout
the last half hour of the flight. During the time before the onset of the
accident sequence, each pilot sought and incorporated information from the
other, and the level of communication and coordination was appropriate for the
task. Captain Germano's statements during the accident sequence were in the
nature of commands and attempts to evaluate the situation and were proper in
that context.
The Boeing February 28, 1996 memorandum to the Chairman of the Human
Performance Group and the September 25, 1996 "contribution" to the Board suggest
that the crew was startled by the wake vortex encounter, perhaps leading to both
crew members manipulating the controls during the wake vortex encounter and
subsequent flight control malfunction. The inference is that the pilots may have
been making contrary control inputs. The inference is not supported by the
evidence, however. The evidence indicates that the pilots were not startled by
this
routine wake vortex encounter and reacted properly to it. In addition, the
speech analysis evidence shows that First Officer Emmett was in physical control
of the aircraft during both the wake vortex encounter and the subsequent attempt
to recover from the uncommanded rudder deflection. The evidence is also clear
that while First Officer Emmett flew the aircraft, Captain Germano properly
provided direction and attempted to analyze the situation. This evidence
indicates the pilots performed their proper duties throughout the accident
sequence, and there was no confusion about which pilot was manipulating the
flight controls.
d. Rudder Pedal Damage Patternsi. Introduction
After admitting there was insufficient pathological information on which to
base an opinion, the Deputy Medical Examiner for the Armed Forces Institute of
Pathology provided an opinion to the Human Performance Group Chairman concerning
the forces being applied to the rudder pedals by the pilots at impact. Because
the metallurgical evidence currently available is at best ambiguous, and the
pathology expert was not qualified to render an opinion on this ambiguous
metallurgical data, no conclusions can or should be drawn concerning the forces
being applied to the rudder pedals at impact. In fact, to the extent a
conclusion can be down from the metallurgical data, it is that a substantial
amount of force was applied to all four rudder pedals and/or their
mounting structures at some point during the impact sequence.
ii. Factual Investigation
Metallurgical examination of the pilots' rudder pedals and mounting hardware
showed that all four of the pilots' rudder pedals bent forward during the impact
sequence. Both pilots' right rudder pedals bent forward 20° and remained
attached to their mounting pivot lugs.
Captain Germano's left rudder pedal sheared from its mounting pivot lug after
also bending forward 20°. First Officer Emmett's left rudder pedal sheared from
its mounting pivot lug after the pedal had bent forward 5°. System Group
Chairman's Factual Report of Investigation, December 21, 1994, Exhibit 9A at 40;
Metallurgist's Factual Report No. 95-43, December 27, 1994, Exhibit 9B, at 1.
The NTSB's metallurgical analysis did not make any findings as to pressure being
applied to the pedals at impact.
Dr. David W. Hause, Deputy Medical Examiner for the Anned Forces Institute of
Pathology, reported that while determination of rudder pedal position can be
inferred from the study of the pilots' remains, the extent of body disruption,
quantity of recovered remains, and incomplete reassociation of the remains in
this case made an analysis based on forensic pathology principles impossible.
Letter from David W. Hause to Malcolm Brenner, Ph.D., January 22, 1996,
Attachment 8 to Human Performance Group Chairman's Factual Report of
Investigation, Fourth Addendum.
Notwithstanding this lack of information, Dr. Hause went on to provide an
opinion to the Human Performance Group in which he "infer[red] the possibility"
that both pilots were "symmetrically applying pressure to their respective left
rudder pedals at the time of ground impact." Id. He based his opinion on
the NTSB's metallurgical analysis of the pedals and attaching hardware. Id.
Dr. Hause claimed he was able to "infer the possibility" that at impact both
pilots were "symmetrically applying" "strong pressure" to the pedals with the
"left knee locked" and "the majority of body weight concentrated on the left
foot. " Id.
iii. Analysis
There is no reason, based on the investigation record, to question the
expertise of Dr. Hause as a pathologist. Indeed, Dr. Hause properly rendered an
expert opinion in the field of pathology when he found there was insufficient
medical evidence on which to determine rudder pressure being applied at the time
of impact. Dr. Hause is not, however, an expert in metallurgy and is patently
unqualified to render an expert opinion based upon metallurgical evidence. Since
Dr. Hause based his inferences on data outside his field of expertise, his
conclusions should be disregarded.
Furthermore, the shear patterns of the rudder pedals on the accident aircraft
are at best inconclusive as to the pressure being applied to them at the time of
impact or at any other point during the impact sequence. The fracture patterns
of the rudder pedal attachment hardware from USAir Flight 427 do not suggest an
application of force by the pilots to any of the rudder pedals. Captain
Germano's left and right pedals bent forward an equal amount (20°), but the left
one sheared off while the right one did not. There is nothing in this pattern to
suggest more pressure on one pedal than the other. First Officer Emmett's right
pedal also bent forward 20° and did not shear off, while his left pedal bent
forward less than 5° before shearing. No metallurgist has provided an opinion as
to the significance of these bending and shearing patterns, but they would not
seem to indicate that one pedal was under greater pressure than the other at
impact, although they may provide some indication as to the relative strength
and flexibility of the attachment hardware. In fact, to the extent a conclusion
can be drawn from the metallurgical data, it is that a substantial amount of
force was applied to all four rudder pedals and/or their mounting structures at
some point during the impact sequence.
It is also significant that the aircraft impacted the ground nose first at
261 knots, approximately 80° nose down, in 60° of left bank, and in a
significant sideslip. A great deal of aircraft structure undoubtedly impacted
the rudder pedals with enormous force as the aircraft telescoped on impact.
Given the left bank and sideslip, it is also probable that the force vectors
would focus more on the left side of the aircraft.Dr. Hause's inferences are
nothing more than unfounded speculation by an unqualified witness based on
ambiguous and inconclusive data. Because the metallurgical analysis currently
available is at best ambiguous, and Dr. Hause was not qualified to render an
opinion on this data, no conclusions can or should be drawn concerning He forces
being applied to the rudder pedals at impact.2. FLIGHT CREW RESPONSE TO
FULL-LEFT RUDDER DEFLECTION
This section addresses the flight crew's response to the full-left rudder
deflection experienced by the accident aircraft. Because the aircraft was at or
near its "crossover speed" (a speed which was not communicated to USAir until
after this accident), and there was no known reason for the flight crew to
maintain or increase airspeed by descending, the aircraft quickly departed from
controlled flight notwithstanding proper efforts by the flight crew to maintain
control. While unusual attitude training is useful and appropriate for airline
flight crews, it would not have affected the outcome of this accident given the
full-left rudder deflection and the accident aircraft's crossover speed.
a. Crossover Speedi. Introduction
Post-accident flight tests conducted in a Boeing 737-300 aircraft revealed
that 190 knots indicated airspeed ("KIAS") was at or very near the "crossover
speed" for the weight and configuration of USAir Flight 427. Below that speed,
ailerons and spoilers are insufficient to stop the roll induced by a full rudder
deflection. Termed the "crossover speed, " this information was not provided to
USAir or the airline industry prior to this accident.When the full-left rudder
movement occurred, USAir 427's flight crew applied lateral controls to
counteract the roll and increased aft yoke pressure to maintain altitude while
they analyzed and corrected the problem. Although this was proper technique,
these actions quickly placed the aircraft in a position from which recovery was
impossible. Unknown to the flight crew and the industry, the aircraft's
crossover speed required an increase in airspeed, and a corresponding loss of
altitude, to accomplish a recovery.
ii. Factual InvestigationAt the beginning of the accident sequence,
USAir Flight 427 was in level flight at 190 KIAS, as directed by Air Traffic
Control. Specialist's Factual Report of Investigation, Cockpit Voice Recorder,
October 5, 1994, Exhibit 12A at 24. Upon acknowledging this speed, the crew of
USAir Flight 427 selected Flaps 1. Id. This configuration was proper
according to both the manufacturer's and USAir's maneuvering speed
schedules.Early in the investigation, the Aircraft Performance Group conducted
tests in the Boeing Multipurpose Engineering Cab ("MCAB") simulator. These tests
indicated that the B-737's
ailerons and spoilers provided lateral control authority sufficient to
counteract a fully-deflected rudder and maintain control of the aircraft.On
October 20, 1994, the FAA began a Critical Design Review of the Boeing 737
flight control system, with emphasis on the lateral and directional flight
controls. Boeing 737 Flight Control System Critical Design Review Report,
May 3, 1995 at 1. The CDR team concluded that a number of possible failure modes
existed in the B-737 which could result in loss of rudder control and subsequent
uncommanded, sustained, full rudder deflection or reversal. Id. at 16.
The CDR team concluded that because of this potential, lateral flight controls
must be "fully available and powerful enough to rapidly counter the rudder and
prevent entrance into a hazardous flight condition. " Id.During its
study, the CDR group conducted tests in the Boeing MCAB sunulator. Id. at
11. These tests provided further data on the aircraft's controllability with a
full, sustained rudder deflection, including rudder hardovers. Id at 12. The
group found that the lateral control system could overcome the roll induced by a
hardover rudder, except at the i90 KIAS/Flaps 1 data point. Id. At this
point, recovery was possible but was very slow and required prompt, precise
pilot control of pitch and airspeed to preclude entering an inverted attitude.
Id. For example, one of the simulator recoveries from a rudder hardover
at the 190 KIAS/Flaps 1 configuration required two separate descents to gain
airspeed, and 35 seconds passed before the simulator was brought under control.
Id. at A-19. The report stated that during this exercise, "recovery from
yaw was in doubt." Id. The amount of altitude lost was not reported.
During September and October 1995, the NTSB, with the participation of USAir,
Boeing, ALPA, the FAA, and NASA, conducted flight tests using a Boeing 737-300
aircraft provided by USAir. One purpose of these flight tests was to verify the
accuracy of the Boeing MCAB simulator's B-737 flight parameters. Berven Tr. at
1973. One data point during the flight test was designed to determine the
aileron and spoiler deflection required to counteract the roll caused by a full
rudder deflection at various airspeeds and flap settings. Id. at 1972.
The flight tests and later engineering analyses revealed that for a B-737
aircraft in the same configuration as USAir Flight 427, there was a "crossover
speed" near 190 knots. ''Crossover Speed" is an engineering term that refers to
the speed at which one set of flight controls exactly offsets the effects of
another set of flight controls, in this case ailerons and spoilers versus the
rudder. Above or below that speed, one set of flight controls is predominant.
Id. at 1980. During the test flights, it was discovered that at speeds
near 190 knots in level, steady-heading side slips, lateral controls (ailerons
and spoilers) were sometimes insufficient to stop aircraft roll induced by a
full rudder deflection. Cox TR at 2161. At the time of the USAir 427 accident,
airline pilots were not trained in or aware of the concept of "crossover
speeds." Cox Tr. at 2191-2. Neither the term nor the concept appeared in
materials the manufacturer provided to the airline industry.
The flight tests also revealed that rudder travel in the B-737 was greater
than that programmed into the Boeing MCAB simulator; that is, the aircraft was
shown to possess more rudder authority than was programmed into the simulator
for the 190 KIAS/Flaps 1 data point. Because of these findings, the MCAB
simulator was modified to more accurately reflect the rudder authority actually
available in the aircraft.
After these modifications, Mr. Berven attempted recoveries in Boeing's MCAB
simulator from full dynamic rudder deflections. Id. at 2021. After the
rudder deflection, Mr. Berven delayed three seconds to simulate a pilot's
recognition time, then started a recovery. If he disregarded altitude loss and
allowed airspeed to increase, the roll typically could be reversed at a 75° bank
angle. When he attempted to keep the aircraft level and maintain 1gO knots, the
aircraft could not be returned to wings level flight -it continued to spiral in
a 70° bank. Id. at 2022. If he allowed the airspeed to accelerate to
above 200 knots, however, the aircraft would begin to recover. Id.
Neither Mr. Berven nor Captain Cox believed a typical airline flight crew
would have attempted to deal with a rudder hardover — assuming they knew such a
malfunction could occur and had a way to recognize it — by descending to
increase airspeed and improve aileron/spoiler effectiveness. Id. at 2036;
Cox Tr. at 2190. Instead, when a pilot is faced with a flight control
malfunction, he or she would instinctively preserve altitude while attempting to
resolve the problem. Berven Tr. at 2037. In fact, prevailing unusual attitude
recovery techniques call for aft yoke pressure when recovering from a nose low
attitude with less than 60-90C of bank.In December 1995, USAir increased by 10
knots its Boeing 737 minimum maneuvering airspeeds for the flaps 1, 5, and 10
settings at gross weights at and below 117,000 pounds. Boeing stated it had "no
technical objection" to these changes, which cleared the way for USAir to
implement the new speeds. Some, but not all operators have followed USAir's
action. Boeing has not affirmatively recommended the changes, stating that the
increase does not provide significant technical benefits to directional control.
USAir also worked to develop a procedure for handling a hardover rudder.
Among other things, the procedure calls for the flight crew to maintain an
airspeed at or above the new maneuvering speed, even if altitude is lost in the
process. That procedure was ultimately incorporated into an FAA Airworthiness
Directive and is now a part of the Boeing 737 Pilot's Handbook.
In June 1997, Boeing provided the NTSB with charts purporting to depict the
effect of bank angle on crossover speeds. This data was not developed as part of
the NTSB investigation and the underlying data and formulae were not provided to
the NTSB. While the charts contain certain anomalies, they do indicate that
B-737 crossover speeds increase with bank angle or, more correctly, with angle
of attack or G loading.
iii. Analvsis
At the time the accident sequence began, USAir Flight 427 was cruising at an
assigned altitude and airspeed of 6,000 feet and 190 KIAS. Commensurate with the
manufacturer's flap maneuvering speed schedule and USAir's B-731-300/400 Pilot's
Handbook, the crew had configured the aircraft with Flaps 1.
Post-accident flight tests conducted in a Boeing 737-300 aircraft showed
conclusively that 190 KIAS was at or very near the "crossover speed" for the
weight and configuration of USAir Flight 427. At this speed, ailerons and
spoilers were sometimes insufficient to stop the roll induced by a full rudder
deflection. Charts Boeing provided to the NTSB in June 1997 suggest that B-737
crossover speeds increase with bank angle (actually angle of attack or G
loading).
Initial investigation efforts in the Boeing MCAB simulator indicated the
aircraft could be recovered from a hardover rudder at 190 KIAS/Flaps 1. However,
this testing occurred before the simulator was modified to reflect the
aircraft's actual rudder authority. Similarly, the FAA Critical Design Review
team found recovery from a full rudder hardover at 190 KIAS/Flaps 1 to be very
difficult in the MCAB simulator. These tests also occurred before the simulator
had been modified to reflect actual B-737 rudder authority. >From the CDR
team's description of the recovery attempts, it is clear that more rudder
authority would have made a successful recovery nearly impossible.
After the Boeing MCAB simulator was modified to reflect the actual rudder
effectiveness found in the aircraft, the FAA's Mr. Berven, one of the pilots who
flew the test flights, experimented with sudden hardover rudder deflections in
the simulator. He concluded that if a B-737-300 aircraft cruising at 190 knots
with Flaps 1 encountered a hardover rudder, recovery was impossible if the pilot
attempted to maintain altitude. Recovery under those conditions was possible
only if the pilot descended to gain airspeed, which decreases rudder
effectiveness and increases aileron/spoiler authority enough to overcome the
roll. However, he also stated that airline flight crews were unlikely to take
such action, as their natural reaction would be to maintain altitude,
particularly while analyzing a control problem.
The manufacturer's pilot handbook for the B-737 did not contain a procedure
for recovering from a hardover rudder. Moreover, the airline industry was not
aware that the manufacturer's recommended maneuvering speed for USAir Flight
427's configuration and weight placed the aircraft at or very near the speed at
which full lateral controls were insufficient to stop the roll induced by a
dynamic hardover rudder or rudder reversal. Indeed, at the time
of the USAir 427 accident, the manufacturer had not informed the airline
industry of the "crossover speed" concept.While unknowingly cruising at or near
the crossover speed for their weight and configuration, the crew of USAir Flight
427 encountered the wake vortex of a preceding aircraft. The Flight Data
Recorder from USAir Plight 427 indicates a full-left rudder movement occurred
approximately four seconds after the wake vortex encounter began. At that time,
the aircraft was in approximately 18° left bank and maintaining level flight.
This uncommanded, dynamic, full-left rudder movement occurred when the aircraft
was at or below the "crossover speed" and an uncontrollable yaw and roll to the
left resulted. The crew's training and piloting sense dictated that they should
maintain altitude while analyzing and correcting the problem, in order to
preserve maneuvering room and available time in which to effect a recovery. At
the onset of the rudder movement, the crew took reasonable action to counteract
the roll with lateral controls while attempting to maintain altitude as they
dealt with the situation. Unknown to the crew, these actions quickly placed the
aircraft in a position from which recovery was impossible. b. Unusual
Attitude Training
i. IntroductionUS Airways believes unusual attitude training is useful
and appropriate for airline flight crews. US Airways has always incorporated
unusual attitude maneuvers, concepts and techniques into its pilot training
programs. In addition, all USAir pilots received unusual attitude recognition
and recovery a number of times prior to becoming airline pilots. In certain
circumstances, unusual attitude recognition and recovery techniques can be
critical to the safety of flight. However, no amount of unusual attitude
training could have prevented this accident.
The full-left rudder deflection combined with the then-unknown crossover
speed of the B-737 aircraft prevented the recovery of Flight 427 notwithstanding
the flight crew's application of proper recovery techniques.ii. Factual
InvestigationThe comments made by the pilots indicate they were fully aware
of the aircraft's attitude, but were unable to change it. Cohen Report at 2.
Captain Cox thought unusual attitude training would not be pertinent if the
unusual attitude resulted from a deflected flight control combined with a lack
of full authority over all three axes of flight. Cox Tr. at 2177.Additional
training in recovery from high bank angle, nose low attitudes has been
considered and implemented by several operators, including US Airways. American
Airlines pilots are taught that when bank angle is less than 60° in a nose low
unusual attitude, the pilot should increase back pressure on the yoke. February
28, 1996 letter from Curt Graeber and Mike Carriker to Malcolm Brenner, at Part
II, No. 17. Flight Safety International recommends that during a nose low
recovery the pilot should increase back pressure immediately if the bank angle
is less than 90°. Id. at 28. US Airways' Selected Events Training program
teaches pilots to apply back pressure in a high bank, nose low recovery after
the bank is reduced to less than 60°.iii. AnalysisAll unusual attitude
training assumes proper functioning of flight controls. Here, the rudder moved
to an uncommanded full deflection at an airspeed which precluded recovery by use
of lateral controls. Unusual attitude training was, therefore, completely
irrelevant because
the aircraft was not responding in a way that allowed recovery by application
of unusual attitude recovery techniques.In any event, the actions of the crew of
USAir Flight 427 conformed with unusual attitude recovery procedures, including
those published after the accident. As the uncorrunanded nodder movement began,
the aircraft yawed and rolled to the left and the nose began to drop. With a
nose low, left bank attitude, the proper procedure is to counter the roll with
opposite aileron/spoiler and increase back pressure on the yoke to reduce
altitude loss, unless the bank angle exceeds 60-90 degrees. This is exactly what
the USAir 427 flight crew did. As the bank angle continued to increase, and the
nose continued to drop, the flight crew disconnected the autopilot, added
additional right aileron/spoiler, and increased back pressure on yoke. This,
too, is consistent with proper procedure. The aircraft reached 60° of bank just
over 5 seconds after the uncommanded rudder movement began, approximately 1 1/2
seconds before the aircraft stalled. At 60° of bank, the flight crew had applied
approximately 2/3 of the available aft yoke authority and full-right
aileron/spoiler, again as appropriate under the circumstances. The aircraft
stalled at approximately 70° of bank, approximately seven seconds after the
full-left rudder movement began.
In hindsight, it can be said that the proper procedure would have been to
increase airspeed by descending until the aircraft accelerated through the
crossover speed. This is not, however, an unusual attitude recovery technique.
It is a technique to recover from a B-737 hardover rudder or rudder reversal. It
is also a technique that is at odds with unusual attitude recovery procedures
and natural piloting instincts.
Because proper unusual attitude recognition and recovery techniques were
followed, and previously unknown factors were at worl: on the aircraft,
additional unusual attitude training would not have prevented this
accident.Under any circumstances then known to the airline industry, the actions
of the crew of USAir Flight 427 were reasonable and correct. Unfortunately, the
crew encountered an unconunanded full rudder deflection at or below the
crossover speed and entered a flight regime wholly unknown at the time to this
crew or the airline industry. Under these extraordinary circumstances, the
crew's application of the correct flight control inputs in an attempt to recover
from an uncornmanded yaw/roll/descent quickly placed the aircraft in an
unrecoverable situation.The actions of this crew cannot be judged with the
benefit of 20/20 hindsight which is itself based on over three years of intense
investigation and analysis. This crew had seven seconds, at most, in which to
recognize, analyze, and recover from a previously-unknown malfunction. Worse
yet, this crew faced the malfunction in a flight regime where recovery was
impossible unless the crew reacted in a way that was contrary to their training
and natural piloting instincts.
CONCLUSIONS
A. FINDINGS
1. The Captain and First Officer were trained, certificated and qualified for
the flight in accordance with applicable regulations.
2. Nothing in the flight crew's background suggests they would have had
problems with disorientation or control of the accident aircraft.
3. The flight crew's performance was not affected by illness, fatigue, or
personal or professional problems.
4. The aircraft was properly maintained in accordance with applicable
regulations. Inspections of the rudder control system required by AD 94-01-07
had been correctly accomplished in a timely manner.
5. It was daylight and the weather was clear with a distinct horizon at the
time of the accident.
6. The accident aircraft's speed and configuration at the beginning of the
accident event complied with the manufacturer's and operator's maneuvering speed
schedules.
7. At the beginning of the accident event, the aircraft was at or below the
"crossover speed," which is the speed below which lateral flight control
authority is insufficient to counter the roll induced by a full rudder
deflection.
8. The manufacturer did not advise the operator, prior to this accident, that
there were speeds below which B-737 lateral flight control authority is
insufficient to counter the roll induced by a full rudder deflection.
9. The manufacturer's published maneuvering speeds for some weights and
configurations of the Boeing 737 were too slow and did not provide sufficient
airspeed margins to allow recovery from an uncornmanded, fully deflected rudder
or rudder reversal.
10. The accident aircraft's rudder moved uncommanded or reversed to the
full-left position.
11. At the onset of the full rudder movement, the accident aircraft's speed
was at or below the "crossover" speed.
12. The manufacturer did not provide the operator, prior to this accident,
with an emergency procedure for recovery of a Boeing 737 from an uncornmanded,
full rudder deflection or rudder reversal.
13. Based on information known to them at the time, the flight crew reacted
correctly to the uncomrnanded, full rudder deflection or rudder reversal and
resultant left roll by selecting opposite aileron and attempting to maintain
altitude.
14. After the onset of the full rudder movement, decreasing airspeed,
increasing bank angle, and increasing aerodynamic loads kept the aircraft's
speed below the "crossover" speed.
15.With an uncommanded, fully-deflected rudder or rudder reversal and the
aircraft below the "crossover" speed, recovery through techniques known at the
time was not possible.
PROBABLE CAUSE
The probable cause of this accident was an uncommanded, full rudder
deflection or rudder reversal that placed the aircraft in a flight regime from
which recovery was not possible using known recovery procedures.
A contributing cause of this accident was the manufacturer's failure to
advise operators that there was a speed below which the aircraft's lateral
control authority was insufficient to counteract a full rudder deflection.
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