New Report Indicates Boeing Reinstalled Alaska Airlines Door Plug

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Key Takeaways:

  • Boeing mechanics in Renton, not Spirit AeroSystems, improperly reinstalled the door plug on Alaska Airlines Flight 1282, failing to install four critical bolts.
  • The incident stemmed from Boeing's poor quality control standards and a missed inspection, according to a whistleblower.
  • In response, the FAA has restricted Boeing's MAX production ramp-up, and Boeing has initiated quality-control focus sessions on its 737 production line.
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The Seattle Times reported today (Jan. 24) that “a person familiar with the details of the work” said Boeing mechanics in Renton, Washington, improperly reinstalled the now-infamous fuselage door plug on Alaska Airlines Flight 1282, a Boeing 737. The Times also reported that the FAA has blocked Boeing’s plan to increase production of the MAXes and approved Boeing’s latest instructions for airlines to inspect the affected aircraft so they can be returned to service.

So far, it has been unclear whether the plug had been installed on the production line at fuselage manufacturer Spirit AeroSystems in Wichita, Kansas, and never removed, or whether Boeing employees had removed the door. The new information indicates Spirit AeroSystems asked Boeing to remove the door plug for rivet work and that Boeing was responsible for reinstalling the panel.

Today’s report supports a narrative last week from another anonymous whistleblower, self-described as a “Boeing insider.” That person said that Boeing’s own records show that four bolts designed to keep the door plug from sliding upward and off the door-frame stop pads were not installed before the aircraft was delivered to Alaska Airlines.

According to the paper, the whistleblower blasted Boeing’s quality control standards: “The reason the door blew off is stated in black and white in Boeing’s own records. It is also very, very stupid and speaks volumes about the quality culture at certain portions of the business.” Though the work should have been verified by a Boeing quality inspector, the whistleblower wrote, the inspection never happened due to a two-system record-keeping process.

Following unusually harsh public criticism from the CEOs of Boeing’s 737 MAX-9 customers Alaska Airlines (Ben Minicucci) and United Airlines (Scott Kirby), Boeing announced that assemblers on the 737 production line would interrupt work on Thursday (Jan. 25) to hold quality-control focus sessions.

Mark Phelps

Mark Phelps is a senior editor at AVweb. He is an instrument rated private pilot and former owner of a Grumman American AA1B and a V-tail Bonanza.
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